Robyn
04-08-2008, 20:02
Recently I became involved with a local fellow that was needing some encouragement along the way on a 6.5 TD overhaul.
This project has spanned many months and a lot of $$$$$$ spent.
The project was in the final stages this past week and a fire was stoked in the little creature. The initial run up proved to be problematic with what turned out to be IP troubles (DS4)
Close to a year of sitting and things did not want to come back to life correctly.
There were a buttload of cylinder imbalance codes and other issues.
After getting involved in a diagnosis it was my opinion that the IP was the culprit and recommended a swap out with a known good one.
I loaned a 5521 that was built in 2000 for the task of diagnostics.
The Ip was switched and the engine fired up and ran fine
NOW the sad tale begins.
The decision was made to run the engine with the intake manifold off to make the task easier so the loaner pump could come off easy and the original rebuilt and replaced or ???
Now the engine runs fine and the tools and such are being put away and things wrapped up for the night.
Just one last run up I am told to enjoy the sweet sound of success.
Not to be.
The valley had been carefully covered with shop rags prior to beding the little beast down for the night.
That one last quick fire up was costly.
The engine lit right off and promptly sucked 2 shop rags in, one into #5 and one into #6 intake port. :eek::eek::eek::eek::eek:
The engine stumbled and shuddered and was shut off quickly.
TOOOOOOOOOOOO late. :(
The results were devastating.
A bent intake valve on each of the holes that sucked a rag.
The number 5cylinder has a crack that is almost the entire length from top to bottom.
The #5hole sucked in enough rag that the piston cocked along the wrist pin axis shoving the cylinder wall out on the outboard side.
The crank apears fine as do all the rods and pistons. (other than 5 )
The #5 rod may be bent I dont know as yet.
The piston looks fine but I would not trust it at this point.
The casualties extended to a bent pushrod on #5 intake too.
The cam shows no sign of damage.
The bearings all look ok other than the #5 rod has signs of the extra stress placed on it during the wreck.
I can't emphasize enough folks that running these with the intake off although quite fine is a risky endeavor unless extreme precautions are taken to rid the engine bay of anything that can get sucked into a port.
There is almost no room in these engines to allow anything to pass through other than air.
This debacle although not the end of the world was costly.
Block, 1 Rod, 1 piston, 1 bearing set, heads maybe (not sure yet) 1 push rod. gaskets and a set of head bolts,1 lifter to be safe. and sundry other little crap to finish the repair.
This was a terrible end to what should have been a 200K engine.
I almost cried when I heard the news. I was on scene to survey the damage the next day and was again on scene last eavening to look over the engine now that its out and apart.
In closing
Any time you have the intake off be Damned sure you dont have stuff like rags or loose parts that can get sucked in.
Any time I need to run one with things open I have a sign taped to the steering wheel (INTAKE OPEN CAUTION) and I keep the keys in my pocket and unhook the battery if I need to leave or have the ports covered with rags or tape.
There is no second chance on this screwup.
Its one way and the outcome is bleak.
My condolences to the poor little creatures owner. He is just devastated.
I understand that a good block has been found and things will progress forward but the hurt on this one will be long and tough to forget.
Please guys, think about this one and pass this along to others that may not read it here.
My Best
Robyn
This project has spanned many months and a lot of $$$$$$ spent.
The project was in the final stages this past week and a fire was stoked in the little creature. The initial run up proved to be problematic with what turned out to be IP troubles (DS4)
Close to a year of sitting and things did not want to come back to life correctly.
There were a buttload of cylinder imbalance codes and other issues.
After getting involved in a diagnosis it was my opinion that the IP was the culprit and recommended a swap out with a known good one.
I loaned a 5521 that was built in 2000 for the task of diagnostics.
The Ip was switched and the engine fired up and ran fine
NOW the sad tale begins.
The decision was made to run the engine with the intake manifold off to make the task easier so the loaner pump could come off easy and the original rebuilt and replaced or ???
Now the engine runs fine and the tools and such are being put away and things wrapped up for the night.
Just one last run up I am told to enjoy the sweet sound of success.
Not to be.
The valley had been carefully covered with shop rags prior to beding the little beast down for the night.
That one last quick fire up was costly.
The engine lit right off and promptly sucked 2 shop rags in, one into #5 and one into #6 intake port. :eek::eek::eek::eek::eek:
The engine stumbled and shuddered and was shut off quickly.
TOOOOOOOOOOOO late. :(
The results were devastating.
A bent intake valve on each of the holes that sucked a rag.
The number 5cylinder has a crack that is almost the entire length from top to bottom.
The #5hole sucked in enough rag that the piston cocked along the wrist pin axis shoving the cylinder wall out on the outboard side.
The crank apears fine as do all the rods and pistons. (other than 5 )
The #5 rod may be bent I dont know as yet.
The piston looks fine but I would not trust it at this point.
The casualties extended to a bent pushrod on #5 intake too.
The cam shows no sign of damage.
The bearings all look ok other than the #5 rod has signs of the extra stress placed on it during the wreck.
I can't emphasize enough folks that running these with the intake off although quite fine is a risky endeavor unless extreme precautions are taken to rid the engine bay of anything that can get sucked into a port.
There is almost no room in these engines to allow anything to pass through other than air.
This debacle although not the end of the world was costly.
Block, 1 Rod, 1 piston, 1 bearing set, heads maybe (not sure yet) 1 push rod. gaskets and a set of head bolts,1 lifter to be safe. and sundry other little crap to finish the repair.
This was a terrible end to what should have been a 200K engine.
I almost cried when I heard the news. I was on scene to survey the damage the next day and was again on scene last eavening to look over the engine now that its out and apart.
In closing
Any time you have the intake off be Damned sure you dont have stuff like rags or loose parts that can get sucked in.
Any time I need to run one with things open I have a sign taped to the steering wheel (INTAKE OPEN CAUTION) and I keep the keys in my pocket and unhook the battery if I need to leave or have the ports covered with rags or tape.
There is no second chance on this screwup.
Its one way and the outcome is bleak.
My condolences to the poor little creatures owner. He is just devastated.
I understand that a good block has been found and things will progress forward but the hurt on this one will be long and tough to forget.
Please guys, think about this one and pass this along to others that may not read it here.
My Best
Robyn