84 Convert
09-30-2006, 20:56
After driving my K2500 I realized something was amiss with the power output of the K30. While I had the truck apart for the valve spring issue, I had pulled the top cover off the IP and discovered metal flakes inside. I also noticed excessive white smoke at idle. My suspicion was the IP being bad, so being that the only known good pump out of the four I have was the -4911, in it went. All I can say is WOW!!
The smoke at idle is GONE, cruise EGT's are down (450 vs 600+ at 60mph), power musta doubled. I now cannot use more than 1/2 throttle without massive black smoke at low rpms. Now I just have to find time and money to complete the turbo setup.
Gregg
The smoke at idle is GONE, cruise EGT's are down (450 vs 600+ at 60mph), power musta doubled. I now cannot use more than 1/2 throttle without massive black smoke at low rpms. Now I just have to find time and money to complete the turbo setup.
Gregg